I tested the motors of the HEX-X drone, but only 5 motors were. Thanks rschoi_75's set-up guide, most of parts are the same, only RX part are different. 6th motor does not work cleanflight2.5.0SPRACINGF3 firmware The program environment used firmware version cleanflight2.5.0SPRACINGF3.hex firmware and configurator 2.6.0. you can check you control command here. Motor Jitter/Start up spinning -> Type: "set motor_pwm_rate=16000" enter. I usually put the Angle mode on AUX2, Horizon on AUX3, Acro/Rate mode if both off. ![]() Acro/Rate mode is the default, so if you wish to use Angle and Horizon, you will need to set it now. It may happen that 0x1C00 is occupied, if BLHeli MAIN was flashed before. Set "ARM" to AUX1 if you wish to arm via AUX1 button. Background: SimonK firmware does jump at run time to a fixed SK-bootloader start address (0x1C00/7168) and tries to check the presents of the bootloader (flash not empty <0xFF). ![]() Min Throttle = 1000, Max Throttle = 2000, Min Command = 1100 You may need to flash older version or build a 'RX_MSP' enable version firmware.ฤก) connect FC using Clean/Betaflight configurator via USB cable (depend on what firmware FC used) Note: remove 'RX_MSP' for all F3 board, which is needed for control from app.
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